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某桥墩桩基偏位分析与纠偏实施效果
引用本文:裴碧峰.某桥墩桩基偏位分析与纠偏实施效果[J].福建工程学院学报,2005,3(4):385-388.
作者姓名:裴碧峰
作者单位:福建建工集团总公司,福建,福州,350001
摘    要:根据桥墩桩基施工现场的具体情况,通过理论计算,分析了两基桩产生偏位的主要原因。采用卸载止推、反向堆载、挖坑卸荷、强力牵拉等综合纠偏方法对产生偏位的两基桩实施纠偏,经过一个多月的缓慢纠偏使两桩基基本恢复原位,纠偏后经桩身低应变动测(反射波法)检测其桩身完整满足设计要求。

关 键 词:墩柱  桩基  纠偏  强力牵拉  卸载止推  抽水减压  反向堆载
文章编号:1672-4348(2005)04-0385-04
收稿时间:2005-04-04
修稿时间:2005年4月4日

Deviation analysis of the pile foundation of a bridge abutment and the effect of deviation-correction
PEI Bi-feng.Deviation analysis of the pile foundation of a bridge abutment and the effect of deviation-correction[J].Journal of Fujian University of Technology,2005,3(4):385-388.
Authors:PEI Bi-feng
Abstract:The main causes for the deviation of two bridge piles were analyzed by theoretical analysis, taking into consideration of the actual conditions of the construction site of the bridge piles. The deviation of the two piles was corrected with integrative correction methods, including unloading stoppage, reverse heap-loading, unloading by digging holes(pits), and forced pooling. With over one month's gradual correction, the two piles'positions were basically restored. The examination of the piles with low strain dynamic measurement reflective wave showed that the piles were complete and met the design demand.
Keywords:abutment  pile foundation  deviation correction  forced pooling  unloading stoppage  pressure-lowering by pumping water  reverse heap-loading
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